Introduction
In 1994 a new palaeoclimatic European Union (EU) project ‘European Project for Ice Coring in Antarctica’ (EPICA) was initiated, in part building on the momentum of the successful European Greenland Icecore Project (GRIP) (GRIP Members, 1993) both in terms of drilling technology and scientific know-how. The plan was to recover deep cores at Dome C (EPICA Dome C (EDC) core (EPICA Community Members, 2004) and in Dronning Maud Land (EPICA DML (EDML) core) (EPICA Community Members, 2006). The Glaciology Group (now the Ice and Climate Group) of the University of Copenhagen (UCPH) that had organized the GRIP drilling project was assigned the task of providing ice-drilling capability for the EPICA project. The drill should also serve the North Greenland Icecore Project (NorthGRIP) (Reference Dahl-JensenDahl-Jensen and others, 2002; NorthGRIP Members, 2004), a new deep drilling project in Greenland, organized and significantly funded by the UCPH group. This opened up the possibility of testing new design features in Greenland prior to the next drilling season in Antarctica, as well as training new drillers for Antarctic work. All these projects became highly successful in terms of drilling performance and scientific outcomes.
The ISTUK drill (Reference Johnsen, Gundestrup, Hansen, Schwander and RufliJohnsen and others, 1994) used in the GRIP project was considered unsuited for the very cold Antarctic temperatures, due to both the battery pack and some special rubber gaskets that would not seal properly at the very low temperatures expected in Antarctica. Thus it was decided to aim at a simpler drill design for the EPICA project. This had been fully specified by the UCPH group when they accepted the task. The EPICA steering committee requested that L. Augustin (L.A.) and P. Journé (P.J.), of Laboratoire de Glaciologie et Géophysique de l’Environnement (LGGE), Grenoble, France, should work with S.J. Johnsen (S.J.J.) and S.B. Hansen (S.B.H.) on the drilling task, and the Italian group from Ente per le Nuove tecnologie, l’Energia e l’Ambiente (ENEA) should build new drill electronics under the supervision of the late N. Gundestrup from the UCPH group, who was also the chairman of the EPICA drilling group.
Successful experiments with the 3 in (7.62 cm) UCPH shallow drill (Reference Johnsen, Dansgaard, Gundestrup, Hansen, Nielsen and ReehJohnsen and others,1980) in a wet hole on Summit Greenland in 1993 pointed to a fully acceptable solution. The shallow drill was modified for drilling in a wet hole by removing the upper half of the 2 m long core barrel and making a space for a chips chamber with a filter at the top. The drive shaft passed through the chips chamber to the core barrel. This design was used in the Icelandic Bardarbunga drill (Ámason and others, 1974; Reference Theodórsson and SplettstoesserTheodórsson, 1976) and was later adopted by the designers of the Japanese Antarctic Research Expedition (JARE) deep drill (Reference Suzuki and ShimboriSuzuki and Shimbori, 1986; Reference SuzukiSuzuki, 1994; Reference TanakaTanaka and others, 1994). In the bottom of the chips chamber a Suzuki booster (Reference HancockHancock, 1994) for compacting the chips was mounted on the drive shaft (Fig. 1).
The test showed that the usual cracking of a dry drilled core after passing a certain depth (presumably due to less manageable and increasingly finer chips) could be entirely prevented, at least to the maximum tested depth of 230 m, by having liquid (D60 lamp oil) in the hole. At these depths the liquid only needs to cover the drill and seems to lubricate the entire chips transport process. Figure 2 demonstrates the core quality before and after the liquid had been added to the hole at 160 m depth.
Main Design Features
Having reviewed existing mechanical drill designs in light of the drilling experience of UCHP, it was decided that the new deep drill for the EPICA and NorthGRIP projects should be based on the same concepts as the Bardarbunga drill (Reference Árnason, Björnsson and TheodórssonÁrnason and others, 1974) as well as on several design features of the ISTUK and UCPH shallow drills (Reference Johnsen, Dansgaard, Gundestrup, Hansen, Nielsen and ReehJohnsen and others, 1980, Reference Johnsen, Gundestrup, Hansen, Schwander and Rufli1994; Reference Gundestrup, Johnsen and ReehGundestrup and others, 1984). The Polar Ice Coring Office (PICO) ice-coring drill (Hancock, 1994) and the JARE deep drill (Tanaka and others, 1994) were designed using similar general concepts.
The main features of the new drill (Fig. 3) were an inner core barrel with spiral flights, a 100 mm drill head scaled up from the shallow drill and an outer barrel with inside grooves. The cuttings were to be stored in a chips chamber at the top of the core barrel. A 30 mm diameter hollow shaft with several holes and a fine-mesh screen (0.5–1.0 mm) clamped on the outside for filtering the chips also acts as a drive shaft extending through the chips chamber. Important modifications were incorporated to ensure fast tripping (better than 1 ms–1) of the drill in the hole, as was the case with the ISTUK drill. This goal was achieved by having a minimum of 5.8 mm clearance between the outer drill barrel and the hole wall. Furthermore, the end pistons of the chips chamber were designed as valves that could be opened (to almost one-third of the drill cross-section) and closed by rotating the drive shaft backwards and forwards. The valves were to be left open until the drilling started, so that, when lowering, the liquid can bypass the narrow, high drag zone between the outer barrel and the hole wall by flowing through a much larger cross-section inside the core barrel and the chips chamber. Easy and fast surface operations were achieved with only two operators, by using the tilting-tower concept of the UCPH shallow and ISTUK drills.
A prototype drill incorporating all these features was built in 1995. The final drawings were made by L.A. with the Euclid drafting program at LGGE in Grenoble. The tubes below the pressure tube along with the inner parts were built by subcontractors in the Grenoble area and overseen by L.A. The drill heads, cutters and shoes were made by H. Rufli (H.R.) in Bern, Switzerland, scaled up from the UCPH shallow drill (Fig. 4). The electronic parts including motor and gear section were imported either from the UCPH shallow drill or the ISTUK drill, and the anti-torque from the ISTUK drill. The overall drill length of 5.0m with the short pressure tube was inspired by the size of an existing drilling tent and also made the drill easily transportable in a Twin Otter or similar aircraft. The drill can also be modified for dry drilling; the only change needed is to mount a specially designed dry drill head with narrower cutters, also made by H.R., giving a minimum of 4mm clearance between the drill and the hole wall. Table 1 lists most of the drill dimensions.
The Hans Tausen Drill Test
Two members of the EPICA drilling group from LGGE (L.A. and P.J.) were invited to participate in the Nordic Hans Tausen Project (Reference Hammer, Johnsen, Clausen, Dahl-Jensen, Gundestrup and SteffensenHammer and others, 2001) organized by the UCPH group, where they assisted S.B.H. and S.J.J. in testing the new drill on Hans Tausen Ice Cap, Peary Land, Greenland.
The drill prototype was equipped with a Suzuki booster and a simple coupling of the core barrel, i.e. no bayonet coupling (cf. Figs 3 and 10). The drill was mounted on the shallow-drill winch base with a 3.5 m long tower and 400 m of cable (Figs 3 and 5a). The electronics were borrowed from the shallow drill, with a 160V d.c. motor mounted inside a short pressure tube on the old ISTUK drill gear section. The anti-torque section was also imported from the ISTUK drill. The drill, tower and general set-up is shown in Figures 5 and 6.
As the HT dry drill head was not ready, the initial dry drilling was done with the UCPH shallow drill down to 106 m. The hole was reamed up to 130 mm with the reamer set seen in Fig. 5a. Three more reamers come with the drill that can ream up to 25 cm diameter for standard casing (Reference Johnsen, Gundestrup, Hansen, Schwander and RufliJohnsen and others, 1994). As very little densifier was available, the drilling liquid used was mainly odourless lamp oil (D60). We never had more than a 50m liquid column in the hole, adding new liquid when the column was lowered to 10 m. There was no casing, so the liquid was dumped in the hole using a 50m long plastic hose. Due to the low liquid density (880 kgm–3), the cuttings left in the hole remained at the bottom for easy retrieval in the next run, a situation the polyethylene spirals and the booster could easily cope with.
The drill test went extraordinary well, almost all the new drilling concepts worked as hoped for and we recovered 344m of perfect core, with typical run length of 1.6 m, during 3 weeks of drilling, working one daily 10 hour shift. Unexpectedly, the core quality turned out to be independent of the liquid pressure at the bottom of the hole. The ice temperature at the ice–bedrock interface was –17˚C. The friction between drill and liquid was very close to what had been predicted by P.J.’s liquid-flow calculations, making 1 ms–1 drill velocity an easy goal to achieve, both when travelling up and down the hole.
One improvement, however, did not work as expected, but taught us a lesson. As an experiment, we extended the flights on the drill head out to the hole wall (Fig. 5b) in order to better guide the cuttings away from the cutters towards the spiral transport system. This ‘improvement’ made the chips pack immediately on the drill head, actually confirming earlier experiences made with the ISTUK drill. New ‘improved’ drill heads, manufactured later in the EPICA drilling project, with more confined conduits for guiding the chips also had the same problem. What we had achieved was to prevent free mixing of fresh cuttings and liquid, which is imperative for proper lubrication and moving of the chips. We also learned later on, when using the pump (discussed below), that the chips–liquid mixture needs constant stirring in order to avoid separation of the two components (ice and liquid), which inevitably results in blocked chip transport, hard packing of the chips on the drill head and a lost run.
Further Developments
During the NorthGRIP and EPICA projects, the drilling group met after each boreal and austral drilling season in order to analyze the lessons learned and to decide on possible improvements to the design. As soon as the highly successful 1995 test field season ended, the drilling group decided that the only change needed for building an efficient deep drill was to make a longer version of the HT drill with all other design features mostly unchanged. The 1.7 m long core barrel and the 1.6m long chips chamber of the prototype HT drill should be made as long as 4 meach in the new deep drill in order to get sufficient core production. This drill was ready for testing at NorthGRIP in 1996 using slightly modified ISTUK electronics and the drill tower from the GRIP drilling project on Summit Greenland. At the same time we tested the new winch intended for the EPICA drilling at Dome C.
The performance of the new drill was far below our expectations. The drilled cores were long and unbroken, but the chip transport between the drill head and the chips chamber was very inefficient, leaving behind too high a proportion of the cuttings from each run, resulting in problems such as difficult penetration. In spite of the problems that summer, however, we installed the casing and managed to drill to 350 m at Summit.
After the field season the drilling group decided on different measures to increase chip transport efficiency, such as stepping up the rotation rate from 60 rpm to 80 rpm and installing more efficient boosters. Another option, not considered feasible by the group at the time, was to build a pump to replace the booster, which in any case is not really pumping liquid but moving and compacting thick slush (as well as dry chips). In fact the spirals are mainly responsible for transporting the chips. Such a pump was, however, designed and built (Figs 3 and 7) by the UCPH group and installed in the drill for the NorthGRIP 1997 season. The pump is a double-action piston pump with two pistons, featuring six 30 mm diameter spring-loaded flap valves each, moving 2 cm in anti-phase inside a special sleeve fixed to the top of the grooved outer barrel (Fig. 7). The pump delivers a maximum 20 L min–1 at 60 rpm rotation speed and allows the liquid to pass through it during descent of the drill. Another obvious advantage of the pump compared to the booster was the ability to keep all the chips inside the chips chamber even after aborted runs with only a half-full and unpacked chips chamber.
The pump immediately improved the performance of the drill and we again recovered long unbroken cores. The drilling was easy, but only just over 90% of the chips in each run were collected. This meant extra cleaning of the hole during night shifts. By going for shorter runs, 3.0–3.5m or so, we would most likely have ensured full chip recovery as was later experienced by the EPICA Dome C drilling crew (Reference Augustin and AntonelliAugustin and Antonelli, 2002). Ease of operation is another important feature of this drill system.
Two HT drills were built, one for the NorthGRIP project and one for the EPICA project (often referred to as the EPICA drill short version). A slightly longer HT-type drill with a 2.14 m long core barrel was also built for the Berkner Island (Antarctica) project (Reference Mulvaney, Alemany and PossentiMulvaney and others, 2007). That drill is also being used in the Italian Talos Dome (Antarctica) drilling project. Two pairs of long deep drills were made for the NorthGRIP and EPICA projects, with slightly different core-barrel/chips-chamber length ratios. The most recently built drills were given longer chips chambers in order to help recover more cuttings. Two of the deep drills were lost by being terminally stuck after hard packing around the drill head and a subsequent failed core break, while most of the short inner parts of the second EPICA deep drill were lost in transit from Dome C. The only remaining NorthGRIP deep drill was used to drill the EDML deep core. A new electronics package (without the batteries of the ISTUK drill) was designed and built for the NorthGRIP/EDML drill by the late N. Gundestrup, F. Wilhelms (F.W.) of the Alfred Wegener Institute, Germany, and S. Sheldon (S.S.) of the UCPH group. The HT drills were also used to deal with the warm ice encountered in both the EPICA and NorthGRIP projects due to their convenient length and easy handling. Without additional remedies the cores drilled close to bedrock were much too short. At NorthGRIP, EDC and EDML, drilling became possible again after a ‘cognac bomb’ (further discussed below) was installed in the chips chamber prior to each run. At EDML, novel modifications were made to the drill head and made the drilling faster. In 2006 the HT drill was used on Flade Isblink, northeast Greenland, for testing new drilling fluids. In the coming years it will also be used to recover new ice cores in Antarctica, on Roosevelt Island and in Aurora Basin. For the next deep drilling in Greenland (North Eemian) we will have to make changes to the NorthGRIP drill in order to cope with the higher viscosity of the new drilling liquids.
Problems with Densifiers
The drilling fluid normally used was D60 mixed with Frigen 141b as a densifier. This densifier has a most annoying property: it sticks to the fine chips and makes them sink to the bottom where they prevent the drilling fluid from mixing with the freshly cut chips, initiating hard packing around the drill head, a situation that can end with a stuck drill. With the pump installed it should be easy to clean the chips from the bottom by lowering the rotating drill slowly so the pump can suck in the chips before touchdown. Initially we planned on having both valves closed and the hollow shaft open while cutting the ice. This configuration works well during drilling but does not work well while cleaning the hole bottom. Cleaning requires the bottom end of the hollow shaft to be closed (e.g. with a spring-loaded ball valve) to prevent the liquid from moving down into the inner barrel and ensure that the circulating fluid goes up the hollow shaft and down the outside of the drill (where cleaning is most needed) and back to the drill head and pump. At the same time the lower valve must be kept open by replacing the upper disc with a ring in order to allow the liquid on top of the core to escape during drilling.
Unfortunately, slow feed-out was not possible with the available winch controller, and the only way to feed cable was to release the brake manually for the shortest possible time. Due to the static friction of the skates, this caused the drill to jump 5–10cm when it finally moved. This intermittent method works well when drilling has started, but often fails to clean the hole bottom properly before cutting starts, as the drill must stop immediately above bottom after the final cleaning slack has been given, and this only happens by ‘accident’. At NorthGRIP in 1997 these unsolved winch problems resulted in a stuck drill at 1372 m.
A new hole was started at NorthGRIP in 1998 using the dry version of the HT drill for drilling the access hole. The dry drilling was fast and stable and the hole was plumb to within a fraction of a degree. The much shorter UCPH shallow drill would normally end up with 2–3˚ inclination at 100 m.
The next stuck-drill situation came up in the year 2000 at 2930 m depth, fortunately in quite warm ice; recovery with (pure) ethylene glycol is quite easy. In EDC the drill got stuck twice in spite of a winch controller capable of slow feed. The second time at 786m in the 1998/99 season resulted in a lost drill (Augustin and Antonelli, 2002). Due to the very cold temperatures, ethylene glycol would not have released the drill. Many runs were lost on this account, but the drillers could somewhat improve the situation by pulling the drill up fast from the bottom with the upper valve closed before starting to drill, in order to mix the bottom chips with more liquid. It was not until 2003 that we had access to a proper winch controller at NorthGRIP, which helped prevent drill sticking during the difficult warm-ice drilling in 2003 and 2004. In the 2001 season we actually had the drill stuck nearly ten times in the warm ice but fortunately it could be released by dumping a few frozen 100 g pellets of pure ethylene glycol in the hole. The pellets would melt in the warm, deep part of the hole and find their way to the hole bottom where they dissolved the packing at the drill head to release the drill.
Glycol was thus an important lifesaver for stuck drills. Having glycol in the hole could possibly have ‘lubricated’ the hole bottom for easier drilling, but eventually when the heavy glycol mixture had dissolved enough ice at the bottom it seemed to become light enough to start moving up into colder ice where it would start freezing out and building annoying glycol/ice bridges that blocked free passage of the drill in the hole (it is also possible that these bridges were leftovers from the 2000 season when an unknown amount of engine antifreeze was dumped in the hole to free the stuck drill).
Spirals
The spirals were initially designed to fill the 4.5 mm wide clearance between the inner barrel and the inside of the grooved outer barrel for moving the chips upwards during drilling. This works well in dry drilling mode, but in wet drilling mode, with the pump installed, the chips/liquid mixture has to be sucked through the three independent channels between the three spirals; fundamentally a most unstable situation as was discovered during the 1997 drilling at NorthGRIP. Many runs were lost when one of the channels became blocked, resulting in packing at the drill head and an aborted run. The solution to the problem was to install thinner spirals. Initially we used 2mm thick wires wound around the core barrel. This worked well, as now there was only one channel leading to the pump and the wires helped stir up the chip/liquid mixture, preventing coagulation of the chips and blocking of the flow. Before installing the wires, an experiment was made to run without any spirals on the core barrel. This failed utterly. Subsequently, the wires were replaced by 2mm thick, 10mm wide aluminium strips. Another experiment, insisted upon by one of the trainees, was to have the strips end at the centring knobs 10cm above the lower end of the inner barrel. In this short interval where the strips were missing, the chips separated from the mixture, resulting in blocked chips transport and immediate packing. The lesson learned was that the chip/liquid mixture needs to be well stirred at all times.
After final tuning of the drill, the 1999 NorthGRIP drilling season produced a record high 1630 m of good core (Figs 8 and 9). Drilling problems were a little more tricky than expected, but our overall mean core production rate was 170mweek–1.
The Bayonet Coupling
The constant threat of a stuck drill in the NorthGRIP drilling project inspired the UCPH group to design a special coupling between the drill and core barrel as shown in Figures 3 and 10. The aim was twofold. First, in a stuck-drill situation, it would make it possible to leave only the core barrel in the hole if all rescue efforts were in vain. Secondly, the coupling could allow an efficient hammer to release the drill when stuck. This feature, however, needs to be further developed. When the NorthGRIP drill got stuck in 2002 we were not able to release the core barrel, as the friction in the rollers was too high and the shear pin in the gear shaft broke. This pin is a leftover from the ISTUK drill, made necessary by the piston-moving screw, but is not needed in the HT-type drills. To use the super-banger/hammer feature of the coupling requires that the electronics can withstand very high g-forces.
Warm-Ice Drilling
Observations made during the GRIP drilling project (Reference Johnsen, Gundestrup, Hansen, Schwander and RufliJohnsen and others, 1994) showed the formation of refrozen water on the cutters at ice temperatures of –10˚C or even colder. The problem did not occur at Dye 3, Greenland, where the basal temperature is –13˚C (Gundestrup and others, 1984); however, at GRIP, as the ice temperature became warmer, up to the maximum of –8.5˚C at the bottom (Reference Johnsen, Dahl-Jensen, Dansgaard and GundestrupJohnsen and others, 1995), the cutters produced a great amount of refrozen melt that would frequently build a bridge between the cutters and channels, blocking the chip transport, producing packing and a short or lost run. Drilling in warm ice thus became a real challenge for the NorthGRIP and EPICA drilling projects, as the bottom temperatures at NorthGRIP, Dome C and DML turned out to be at the pressure-melting point, ~–2.4˚C.
The problem was first encountered at NorthGRIP during the 2002 season. We had some ethylene glycol in the hole but it did not seem to ease the meltwater problem (although it certainly helped to release the drill every time it got stuck). Another problem was the sticking of the core in the core barrel due to freezing of the glycol mixture (and later the ethanol mixture) between the core and core barrel during pull-up. The solution was to first heat the entire drill inside a long box with warm air from a Hermann–Nelson blower and, when the core barrel was released, to heat the barrel in a D60 bath to a temperature close to the actual temperature during drilling.
The warm ice became difficult to drill at Dome C in the following, 2002/03, drilling season (Reference Augustin, Panichi and FrascatiAugustin and others, 2007). The drilling group had recommended that ethanol be brought to Dome C to help cope with the meltwater and subsequent freezing on the drill and core. This turned out to be a most difficult venture as, although the ethanol water solution (EWS), brought to the bottom of the hole, initially helped the drilling, most of the EWS unexpectedly turned into great amounts of ice–ethanol slush obstructing the drilling until it was cleaned out.
At NorthGRIP the warm-ice problem was first seriously attacked in the 2003 season. We brought a heated isolated tank to bring EWS to the bottom and we also brought an ethanol thermal drill (Reference Zagorodnov, Thompson, Mosley-Thompson and KelleyZagorodnov and others, 2002). We hoped the thermal drill would be ideal for drilling in ice close to the pressure-melting point. Our initial experiments resulted in the following outcome. Firstly, the ethanol brought down to the bottom in the tank behaved much worse than we had expected, eventually turning into slush, inhibiting further proper drilling. Secondly, the spiral heater at the lower end of the thermal drill burned out as soon as the drill touched bottom, most likely due to extremely high voltage (in the megavolt range) between the NorthGRIP camp and the (pink electrolytic) water in the ice matrix in galvanic contact to bedrock.
The ‘Cognac Bomb’
Based on the difficulties experienced so far with using EWS to deal with the warm ice, it was decided to deliver only a limited volume, around 0.5–1 L, of about 50% EWS with the drill in each run. The aim was to drill enough core during the run to recover most of the EWS brought down in the chips chamber to prevent excessive formation of slush. The EWS was stored in a 5 cm diameter, 0.5 L, plastic hose, the ‘cognac bomb’ closed with two knobs and clamped to the hollow shaft of the HT drill with hose clamps (Fig. 11a). When the drill motor was started, the plastic hose was ripped open just above bottom by a pointed screw extending through the wall of the chips chamber. The pump would then ensure that the released EWS would circulate down to the drill head and prevent or slow down refreezing of the meltwater produced by the cutters. The drilling, however, did not become stable until some non-magnetic nuts and screws had been removed from the bottom of the hole using a newly built vacuum cleaner (Fig. 11b). The ‘cognac bomb’ worked much better than earlier experiments with EWS, and the drillers became much happier, as Figure 12 clearly indicates. We were able to drill up to 5 m of good core daily down to 3085 m depth, when the bottom meltwater flushed the hole, immersed the drill and shorted the electric connections in the anti-torque section.
In 2004 the drilling was continued in order to recover the 45 m of refrozen bottom water from the previous year. By using the same ethanol procedure as in the previous year and the same winch controller, the drilling went on in a stable routine and bedrock was reached at 3090.5 m, 5.5m below the water channel we drilled into the year before.
The Ultimate Lesson Learned
During decades of drilling in polar ice, one lesson we have learned stands out as being the most important. It often happens that a mistake is made or something goes wrong with the mechanics or the electronics. The operator will then quite often be tempted to play the hero and go for a quick fix of the apparent problem. He may be lucky and all goes well, but more often, by not having analyzed the event thoroughly in an open discussion with those who know the system, he will misunderstand the situation and make a wrong decision. Such decisions will frequently produce damage an order of magnitude worse than if a decision had been made based on a sound understanding of the problem. The scenario is like the second-impact damage in a car accident. When bad things happen (and they will), take a break and discuss the problem in the open before any action is taken.
Acknowledgements
We are greatly indebted to the various funding agencies for supporting the projects involved, including the cost of drill development and drilling. We also thank all the logistic people for organizing the field camps and for bringing us there along with our equipment. The numerous drillers who put long cold hours into careful drilling and recovery of good-quality cores are thanked for their vital contribution, and for helping to improve the drills and drilling techniques. Finally we thank the scientific teams for making such good use of the ice cores we managed to deliver. To drill good ice cores against all odds is a most satisfying experience in a well-functioning drilling camp, but to see the final outcome described in high-level scientific papers should also be a fully acceptable reward.