Introduction
On 16 December 1957, during the International Geophysical Year (1957/58), Vostok station (78˚28' S, 106˚48' E; 3488m a.s.l.) was established near the South Geomagnetic Pole, the point where the Earth’s magnetic dipole axis crosses the Earth’s surface Fig 1. The South Geomagnetic Pole, like the South Magnetic Pole, changes through time, although more slowly. For example, in mid-1996 the South Geomagnetic Pole was situated at 79˚18' S, 108˚30' E, approximately 100 km from Vostok. Since 1957, Vostok has existed as a year-round research base of the Complex Antarctic Expedition (CAE). In 1959 CAE was renamed the Soviet Antarctic Expedition (SAE). After the collapse of the USSR, the Russian Federation assumed obligations relating to the Antarctic Treaty, and on 7 August 1992, according to Edict No. 824 of the President of the Russian Federation, SAE became the Russian Antarctic Expedition (RAE).
The first ice-drilling experience took place at Vostok in 1958, when wintering-over personnel received a message from the 4th CAE to start drilling into the ice sheet. Nine thermal-drill types were designed from makeshift material and equipment found at the station. All of them were finally frozen in the ice. Nevertheless, four boreholes were drilled to a maximum depth of 52 m Fig 2.
In 1963, a research agreement between the Arctic and Antarctic Research Institute (AARI) and two Moscow research institutes – the Moscow Mining Institute and the Moscow Institute of Radio-electronics and Mining Electromechanics – led to the design of a thermal ice-drilling system. In 1967 a collaboration between AARI and the Leningrad Mining Institute (LMI) led to development of the thermal coring drill for drilling in dry holes. Later, further improvements were made under a new cooperative venture between AARI and LMI.
During the winter of 1969 (14th SAE) two test holes were drilled near Mirny station and a 250 m deep hole was drilled in 36 days at the 50 km mark of the Mirny–Vostok traverse. In 1970, 12 years after the first experience, drilling at Vostok station was conducted by LMI specialists. (In 1991 LMI was renamed the St Petersburg State Mining Institute (SPSMI)). Since 1970, five deep holes have been cored: hole No. 1 to 952 m; hole No. 2 to 450.4 m; hole No. 3G (3G-1, 3G-2) to 2201.7 m; hole No. 4G (4G-1, 4G-2) to 2546.4 m; and hole No. 5G (5G-1) to 3650.2 m depth.
In the mid-1990s, the existence of a large subglacial lake beneath the Antarctic ice sheet (since named Vostok Subglacial Lake – its south part underlies the station) was recognized (Reference Ridley, Cudlip and LaxonRidley and others, 1993). Previously, the primary objective of deep ice-core drilling at Vostok was to acquire englacial geophysical data and a long ice core for studies of past climate history. Now, the primary interest is to study the lake properties using the existing hole No. 5G-1.
In this paper, we recollect our successes and problems including the reasons for accidents, some of which have not previously been published. Even for those that have been published, descriptions of drilling operations have mostly been in Russian and not available for the English-reading scientific community. Most of the photographs are published here for the first time. The last part of the paper is devoted to our plans for penetrating and sampling Vostok Subglacial Lake.
Drilling Operations in Hole no. 1 (1970–73)
15th SAE (1970)
In the summer season of the 15th SAE, the first drilling shelter was constructed on two steel sleds Fig 3, providing a work area measuring 15×2.9×2.5 m. A 9.7m round tower, measured from the top of the hole, was constructed in the center of the work area and wrapped in rubberized cloth for protection Fig 4.
The first attempt at deep-hole drilling at Vostok began in April 1970 using the thermal drill, TELGA-14, previously tested at Mirny station. In this drill, meltwater was removed by a vacuum system and collected in a tank (Fig. 5; Table 1). A dry hole, hole No. 1, reached 506.9 m by September 1970 (Table 2). In total, 293 drilling runs were completed (Reference BarkovBarkov, 1970; Reference Barkov, Bobin and StepanovBarkov and others, 1973; Reference Kudryashov, Fisenko, Stepanov and BobinKudryashov and others, 1973a, Reference Kudryashov, Bobin, Slyusarev, Stepanov, Fisenko and Chistyakovb).
The most serious difficulty encountered during drilling was contamination of the hole by impregnated graphite escaping from beneath the cable armor. The graphite settled to the bottom of the hole and impaired the heat transfer from the heating head to the ice, reducing the penetration rate by 20–30%. A special, conically shaped, 3 kW heating head was used to melt a depression at the bottom of the hole into which the graphite settled. After the meltwater had frozen, the ice containing the contaminant was removed as part of a core. This procedure was repeated at depths of 276, 346, 419 and 498 m. The contaminant also coated the walls of the water suction tubes and impaired the operation of the pump; both the suction tubes and pump had to be periodically cleaned. Drilling progressed slowly, without further serious complications except for two mishaps (Reference Fisenko, Bobin, Stepanov, Slyusarev, Solov’ev and ChistyakovFisenko and others, 1974).
The first occurred at 15.7m depth owing to a switch malfunction. A section of the drill broke off at the balance block and fell down the hole. It was retrieved using an adapter on the end of a column of rods, which was threaded into the broken section. The operation took about 6 hours.
At 497.4m depth, a 20 cm steel rod was accidentally dropped to the bottom of the hole. A special heater assembly was used to melt a small central hole, which repositioned the rod from an inclined to a more vertical position. In this position, the rod would fit within the annular heating head of the TELGA drill. It was then recovered atop the next core. The operation took 14 days.
16th SAE (1971)
Drilling of hole No. 1 was continued. At the beginning of winter, due to carelessness, the TELGA-14 drill, unattached to a cable, was dropped to the bottom of the hole. It was recovered using special grips (Reference Fisenko, Bobin, Stepanov, Slyusarev, Solov’ev and ChistyakovFisenko and others, 1974). Later, at 560 m depth, as the drill was being hoisted, it became stuck near the bottom of the hole, probably because of the inadequate removal of meltwater. A whip-stock 4.5 m long was set at 505 m depth, and directional drilling began using a short thermal drill (total length 2 m) with a conical drill head.
A new offset hole was started from 518 m depth (Fig. 6). To ensure free passage of the longer thermal drill, the deviated interval of the hole was enlarged, but unfortunately the old hole was reopened in the process. From that time on, the drill sometimes entered the new hole and sometimes the old one. At 534.4m depth, drilling of the offset hole was stopped. The bottom part of the hole was filled with ice up to 471 m depth and a new directional drilling effort was started without using a whip-stock. The deviation was accomplished using a thermal drill with a special asymmetrical thermal head. By the end of winter, the depth of hole No. 1 reached 625.2 m.
17th SAE (1972)
Drilling of hole No. 1 was continued using the modified thermal drill TELGA-14M. From 920m depth, drilling was conducted using a spliced cable because the necessary length of cable was not available at the station. The lowering and hoisting was accompanied by repetitive jerking and sticking in the narrow parts of the hole (occurring 30 times during one run). Nevertheless, the hole reached 952.4m in May 1972, making it the deepest dry hole in ice (Reference Korotkevich and KudryashovKorotkevich and Kudryashov, 1976; Reference KudryashovKudryashov, 1989). The final run occurred while the drill was being lowered to the bottom of the hole, when the winch-brake mechanism failed. The drill dropped to the bottom of the hole followed by the cable, which eventually became detached from the clamp holding it to the winch drum and fell into the hole. The drill and cable were eventually left in the hole.
A new offset hole was started. A cylindrical piece of ice was dropped from the surface into the hole, but unfortunately it got stuck at 30m depth and efforts to dislodge it failed (Reference Fisenko, Bobin, Stepanov, Slyusarev, Solov’ev and ChistyakovFisenko and others, 1974). From this depth, a new offset hole, hole No. 1-bis, was started and by the end of the year reached 774m depth (Reference Kudryashov, Chistyakov and VartykyanKudryashov and others, 1975, Reference Kudryashov, Chistiakov and Bobin1977).
18th SAE (1973)
The drilling in hole No. 1-bis was continued through the interval 774–780.2 m, at which point the hole became inaccessible owing to an accident during hoisting. The thermal head was stuck near the bottom and separated from the drill at 762 m depth. The drill itself then became stuck at 308 m depth (Reference Vartykyan, Kovalenko and MoiseevVartykyan and others, 1977). The main reason for the accident was the inexperience of the new team, who did not recognize problems with the pumping of meltwater at the bottom of the hole. Ultimately, this led to the drill becoming stuck during hoisting (the drill profile ‘swelled’ because of refrozen water on its surface) during one of the first runs carried out by the new drilling team of the 18th SAE.
A new offset, hole No. 1-2bis, was started at 307 m depth in hole No. 1-bis and reached 905m depth (Kudryashov and others, 1977, Reference Kudryashov and Yakovlev1991). Further drilling in this hole was stopped owing to the high risk of getting the drill stuck. Hole No. 1 -2bis was available for several years for scientific observations of temperature, deviation from the vertical, and wall deformation (Reference Dmitriev, R.N. and I.A.Dmitriev and others, 1978).
Drilling Operations in Hole no. 2 (1971–76) and Experimental Holes (1977–79)
16th SAE (1971)
During the summer season, the drilling shelter was reconstructed and extended to a length of nearly 30 m (Fig. 7). A special square tower 17.7m high was built in the central part of the extended building. From this new set-up, an experimental hole, No. 2, was drilled to 108 m using a TELGA-14 thermal drill. The primary purpose was to drill a start-up hole for testing a new electromechanical drill, KEMS-152. The experiments were not carried out, because of imperfections in the new drill (Kudryashov and others, 1973b).
19th SAE (1974)
A casing was set in place in hole No. 2. It was made from steel tubing with an outer diameter (OD) of 168 mm and inner diameter (ID) of 154 mm. The main problem was sealing the lower part of the casing to the ice. Water was poured into the hole from the surface. Hardly any of it reached the bottom, because most of it froze on the inner surface of the casing.
After the casing was cleaned, the hole was filled with a water–ethanol solution. The first attempts to drill in a deep fluid-filled hole using a TBZS-152 thermal drill (Fig. 5b; Table 1), with a water–ethanol solution as the fluid, encountered many problems. Owing to the dissolution of ice from the borehole walls, the water–ethanol solution decreased in concentration and formed an icy slush, which hindered drill penetration. In total, the depth interval 108– 142m was drilled with a mean ethanol consumption of 50 Lm–1 (Reference Kudryashov, Chistyakov and MorevKudryashov and others, 1983, 1991; Kudryashov and Yakovlev, 1991).
20th SAE (1975)
The drilling liquid in hole No. 2 was changed to a kerosene-based aircraft fuel, TS-1. During drilling, the liquid level was kept at 130–150m depth. Drilling continued with the same TBZS-152 thermal drill down to 450.4 m, where the drill became stuck, most likely because of problems in the water removal system (Reference Zagrivny, Zemtsov, Kononov, Moiseev, Petukhov and ShkurkoZagrivny and others, 1981; Kudryashov and others, 1983). The cable was ruptured during the attempt to free the drill.
In the interval 142–450.4 m, 199 drilling runs were completed. The power of the copper drill head was 6 kW, and the power of the aluminum drill head was 5.3 kW. The power of the heating elements in the water suction tubes was 120Wm–1; the power of the heating elements in the water tank was 1.5 kW per meter of water column (Reference Zagrivny, Zemtsov, Vostretsov and ShkurkoZagrivny and others, 1980).
21st SAE (1976)
A new offset hole, No. 2-bis, was started at 224m depth in the original hole No. 2 but the drill became stuck again. The final depth of hole No. 2-bis was not reported. According to our personal recollections, only a few runs in the new offset hole were made.
22nd SAE (1977)
Experiments with a TBZS-152 thermal drill were continued. Two unnumbered holes with depths of 171 and 300 m were drilled. Drilling was difficult, and a few serious accidents occurred. Drilling at Vostok was suspended in order to improve and test the technology of fluid-filled drilling. Such experimental drilling has been carried out on Vavilov glacier, Severnaya Zemlya archipelago, Russia, (Reference Chistyakov, Shkurko, Zemtsov, Vasiliev and Solov’evChistyakov and others, 1988) and, during the wintering of the 24th SAE at Gornaya base, at the 73 km mark of the Mirny–Vostok route (Reference Kudryashov and YakovlevKudryashov and others, 1991).
Drilling Operations in Hole no. 3G (1980–86)
25th SAE (1980)
The mobile drilling shelter, PBU-2, utilized for drilling at Gornaya base was towed to Vostok (Fig. 8) and used for drilling a new deep hole at Vostok station. The first 112 m of the new hole, No. 3G (G is the first letter of the Russian word glubokaya – ‘deep’), was drilled as an uncased, dry hole using a TELGA-14M thermal drill. Below the firn–ice transition, the TBZS-152M thermal drill was used in a fluid-filled hole, the fluid consisting of aviation fuel TS-1 with densifier CFC11. The hole was extended to 1351 m by 17 December 1980 (Kudryashov and others, 1983, Reference Kudryashov, Chistyakov, Zagrivny and Lipenkov1984a, Reference Kudryashov, Chistyakov and Bobinb, Reference Kudryashov, Chistyakov and Litvinenko1991; Reference KudryashovKudryashov, 1989; Reference Kudryashov and YakovlevKudryashov and Yakovlev, 1991).
26th SAE (1981)
The drilling of hole No. 3G was continued with a TBZS-152M drill over the interval 1415–1500 m. Beyond this depth, the TBS-112VCh thermal coring drill (Fig. 5c; Table 1) was used. This drill used a high-frequency power supply, which reduced the dimensions of the electric transformers positioned in the drill. At the surface, the power supply had a frequency of 2500 Hz and voltage of 800–1000V. Passing through the cable, the electric voltage dropped to 700– 900V. At the bottom, this primary voltage was reduced by electric transformers to the voltage of 20–25V used in the drill. The water tank was not heated. The meltwater was collected in a tank and frozen inside. At the surface, the tank was removed and replaced with an empty tank. The core barrel was made from a thick-walled tube, with the water suction tubes and the electrical lines hidden within the wall.
The drilling rate was doubled to 3.5–4mh–1 over the TBZS-152M with 5 kW of power. After reaching 1580m depth, owing to problems with the meltwater removal system, the drill became stuck near the bottom of the hole. A new offset hole was started using another TBS-112VCh thermal drill with a length of 7.1 m at 1500m depth, and in the interval 1550–1560m a full-diameter core was recovered (Reference Zagrivny and MoiseevZagrivny and Moiseev, 1988). The new offset hole was designated hole No. 3G-1. A depth of 2004m was reached by the end of the summer season (Kudryashov and others, 1984a, Reference Kudryashov and Yakovlev1991; Reference Zagrivny, Moiseev and ShkurkoZagrivny and others, 1985; Reference Kudryashov and YakovlevKudryashov and Yakovlev, 1991). Labeling of the ice core was kept as No. 3G down to 2083 m, the end of hole No. 3G-1.
27th SAE (1982)
In early 1982, hole No. 3G-1 was advanced to 2083 m with a TBS-112VCh thermal drill (Zagrivny and others, 1985). A generator-room power-station fire on 12 April 1982 tragically took the life of the chief mechanic and curtailed further drilling (Reference Kudryashov and YakovlevKudryashov and others, 1991). On 26 December 1982, another fire destroyed the drilling shelter PBU-2 which housed the drilling complex for hole No. 3G, and drilling was suspended.
29th SAE (1984)
The mobile drilling complex PBU-3, which was transported from Mirny during the 28th SAE, was installed above the mouth of hole No. 3G (Fig. 9), replacing PBU-2 which had been destroyed by fire. The drilling operations in hole No. 3G-1 were resumed with a TBS-112VCh thermal drill, but the lower part of the hole had closed in during the long period of inactivity. During the enlarging or reaming process, a new offset hole was accidentally started at 1968.5 m depth. It was designated hole No. 3G-2 and was advanced to 2040 m(Reference Kudryashov and YakovlevKudryashov and others, 1991). Ice-core labeling was No. 3G-1 down to 2202 m, the end of hole No. 3G-2.
30th SAE (1985)
Drilling in hole No. 3G-2 was resumed. A TBS-112VCh thermal drill reached 2201.7m in August 1985 for a new ice-core drilling depth record (Reference KudryashovKudryashov, 1989). The drilling was going on with continual enlarging of narrowing parts of the hole. Drill thermal heads were not properly adapted to the high hydrostatic pressure of drilling fluids, which led to premature burning of heating elements. In total, nearly 75 thermal drill heads were used in the last interval, 2040–2201.7 m.
31st SAE (1986)
The TBS-112VCh thermal drill was stuck in hole No. 3G-2 during enlarging operations in the interval 1935–1943m (Reference Kudryashov and YakovlevKudryashov and others, 1991). Further activity in hole No. 3G-2 was stopped.
Drilling Operations in Hole no. 4 (1982–89)
27th SAE (1982)
The construction of a new stationary drilling complex was started for a new hole, No. 4G. It was built on two steel sleds with a 15 m mast, and 4000m of a KG-95-180 type, seven-conductor armored cable (Reference KudryashovKudryashov, 1989).
28th SAE (1983)
The construction of a new drilling complex was finished by 29 May 1983 (Fig. 10) and the new hole, No. 4G, was started on 3 July. Drilling in holes No. 3G and No. 4G overlapped by several years due to the efforts of two different shifts. The 178mm diameter hole reached 120m using a TELGA-14M thermal drill. After the hole was filled with liquid, a TBZS-152M thermal drill was used to advance it to 279m by the end of the season, 12 February 1984 (Reference Kudryashov and YakovlevKudryashov and others, 1991).
29th SAE (1984)
Problems with the winch (the bolts of the winch drive-shaft coupling failed) used for hole No. 4G resulted in the loss of the TBZS-152M drill at the previous season’s depth of 279 m (Reference KudryashovKudryashov, 1989). Further drilling operations in hole No. 4G were curtailed.
30th SAE (1985)
The lost drill in hole No. 4G was bypassed with an offset hole No. 4G-1 started at 120m by a TELGA-14M thermal drill; drilling continued to 167 m and then to 692 m depth with a TBZS-152M thermal drill (Reference Kudryashov and YakovlevKudryashov and others, 1991). Unfortunately, the initial hole was not packed with ice before deviation, which caused many problems thereafter.
31st SAE (1986)
Hole No. 4G-1 was advanced to 752 m with the TBZS-152M thermal drill. The old hole, No. 4G, was accidentally reopened because of the absence of ice plug at the place of deviation. This made it impossible to return to hole No. 4G-1, so a new offset hole, No. 4G-2, was started from hole No. 4G at 159 m. A depth of 779m was reached by 26 December 1986. Owing to inadequate centering of the drill, the inclination of hole No. 4G-2 reached 18˚ in the depth interval 500–600m (Reference KudryashovKudryashov, 1989; Reference Kudryashov and YakovlevKudryashov and others, 1991).
32nd SAE (1987)
Drilling in hole No. 4G-2 continued with a TBZS-152M drill to 1502 m (Fig. 11). In order to reduce hole inclination, the interval 779–936m was drilled with a shortened version of the TBZS-152M thermal drill (Reference Kudryashov and YakovlevKudryashov and others, 1991). The shortened version of the drill could penetrate with a smaller angle between axis of the drill and the vertical, allowing a reduction in the inclination.
33rd SAE (1988)
The continuation of drilling in hole No. 4G-2 with the TBZS-152M drill passed 2213m by 1 November 1988, thereby exceeding the old record, and reached 2383 m by the end of the season. The hole inclination did not exceed 4˚ (Reference KudryashovKudryashov, 1989).
34th SAE (1989)
Deep drilling of hole No. 4G-2 using the TBZS-152M thermal drill was stopped at 2428.5 m in April 1989 owing to hole closure caused by a deficiency in fluid pressurization. Attempts to increase the density of the hole fluid with a high-density additive were not fully successful.
In June 1989, drilling resumed with an electromechanical drill referred to as KEMS-112 or KEMS-132 (KEMS-135) depending on ODs of the core barrel and the drill-head cutters (Fig. 12; Table 1). The upper part of the drill (motor-gear section, pump, cable termination, etc.), except the skates of the anti-torque sections, is the same in all versions of the drill. The lower part of the drill (core barrel and chip chamber) of the KEMS-112 type is assembled from steel tubes with OD/ID of 108/99 mm, and the KEMS-132 (KEMS-135) from tubes with OD/ID of 127/117 mm. The drive motor for either design was three-phase, 220V, with a capacity of 2.2 kW. A two-stage gear reducer lowered the speed from 2800 rpm to 230 rpm. Testing had been conducted in the Arctic prior to the drilling at Vostok.
In the first 20 runs, the length per run was <0.1 m. The drill was stuck at 2431.7 and 2437.5 m, but freed in 5 days and 2 hours, respectively. After every 10–15 m, the hole was enlarged with a 135 mm cutting head. At 2546.4m depth, drilling was interrupted for 16 days and a new 4000m long cable was installed. The drill became stuck on the first run, 1 m above the bottom. The operation was left for a year with tension on the cable (Reference Vasil’yev, Kudryashov, Talalay and ChistyakovVasil’yev and others, 1993; Reference Kudryashov, Vasiliev and TalalayKudryashov and others, 1994).
35th SAE (1990)
The drilling complex was moved. A small shelter with pulling equipment was built above the mouth of hole No. 4G. The drill was still stuck in the hole. During a recovery attempt, the cable failed near the surface in November 1990 (Kudryashov and others, 1994).
Drilling Operations in Hole no. 5G (1990–2006)
35th SAE (1990)
In January 1990 the drilling complex was moved 25 m to the west (Fig. 13 shows the drilling shelter as it appeared during SAE-35). A new hole, No. 5G, was started on 20 February 1990, using a TELGA-14M thermal drill to 120m depth in 62 runs (Fig. 14). Beyond this depth, another thermal drill for fluid-filled holes, TBZS-152M, was used. A depth of 1279.8m was achieved in 398 runs with the TBZS-152M drill by the end of the season, 29 January 1991 (Reference Tchistiakov, Kracilev, Lipenkov, Balestrieri, Rado and PetitTchistiakov and others, 1994; Reference Kudryashov, Chistyakov, Vasiliev and VolkovKudryashov and others, 1998a, Reference Kudryashov and Hallb, 2002).
36th SAE (1991)
Drilling in hole No. 5G reached 2502.7m in December 1991, with the TBZS-152M thermal drill completing 408 runs. The round-trip time to the bottom of the hole and back increased to 2.6 and 1.8 hours respectively, at 2500 m depth. The inclination varied between 0.2˚ and 0.6˚ down to 2000 m, then increased gradually from 0.4˚ to 1.8˚ at 2250 m. At the end of December, the drill became stuck at 2259m during a trip up-hole. The problem was caused by hole closure from insufficient fluid pressurization. All attempts at recovery failed and the cable was pulled out of the top of the drill (Tchistiakov and others, 1994; Reference Dmitriev, Zubkov, Krasilev, Menshikov and PashkevichDmitriev and others, 1995; Kudryashov and others, 1998a, b, 2002).
37th RAE (1992)
Densifier HCFC 141 b was added to hole No. 5G, increasing the fluid density to 900 kgm–3. About 35 m of artificial core was dropped on top of the stuck drill, creating a new hole bottom at 2232 m. A shortened version of the TBZS-132 thermal drill, 6m long, was used to drill a new offset hole, No. 5G-1. From 2249.5m depth, drilling was continued with a TBZS-132 drill with a normal length of 8m, to 2270.7 m depth by the end of the winter and to 2341.8 m by the end of the summer season. The main differences between the TBZS-132 and TBZS-152 thermal drills were the OD and ID of the drill head and the tubing used for the core barrel and water tank (Kudryashov and others, 1998a, b).
38th RAE (1993)
From August 1993, following the collapse of the USSR, ice coring and core research at Vostok station was conducted by a joint Russian–French–US project. The Russians maintained the station and conducted the drilling operations, the French provided technical equipment and the Americans provided logistical support. Since that time, the core has been divided between the three partners to the agreement.
Hole No. 5G-1 reached 2755.3 m depth with the TBZS-132 drill. The depth was a new record for thermal drilling in ice. From 18 September 1993, drilling ceased because the supply of drilling fluid was exhausted (Kudryashov and others, 1998a, b, 2000, 2002).
39th RAE (summer season 1993/94)
During the summer season, the upper part of hole No. 5G-1 was enlarged from 180 to 220 mm using an electromechanical reaming technique. The hole was cased with fiberglass tubing and, using a thermal shoe at the bottom of the casing, it was sealed at 120m depth so that hole fluid could be retained throughout the permeable zone. The OD/ID of the casing tubes was 179/165 mm. The OD of the connecting couplings of the 6m long sections was 215 mm. It was discovered, however, that fluid could only be maintained to a maximum height of 66m below the surface, owing to a leak at an uncertain location (Kudryashov and others, Reference Kudryashov, Vasiliev, Zubkov, Krasilev, Nikishin and Chistyakov2000, Reference Kudryashov2002). On 10 February 1994, Vostok station was temporarily closed for the winter for logistical and economic reasons.
40th RAE (1995)
On 22 November 1994, the traverse from Mirny reached Vostok, and on 27 November the station was fully reopened. Drilling operations in hole No. 5G-1 were resumed. First, to compensate for the ice overburden pressure, the density of the drilling fluid in the hole was increased. Then the hole was enlarged between 2200 and 2755 m from 134 to 139mm in diameter with an electromechanical reamer to facilitate lowering and raising the drill. Drilling began with the KEMS-132 electromechanical drill in February 1995 and reached 3109 m depth in September 1995, when the drilling was stopped because all of the densifier supply had been consumed. An average drilling run of 2.8m was achieved, but beyond 2930 m the length of the drilling runs decreased dramatically because of sticking and jamming of the drill (Kudryashov and others, 1998a, b, 2000, 2002). The temperature in the hole at 2930m depth was near –20˚C (Fig. 15), too cold to consider ‘warm ice’ as the main reason for complications. Partially our problems can be explained by changing ice properties, in particular changing ice crystal size (see below).
41st RAE (summer season 1995/96)
A supply of the densifier HCFC 141b was delivered to the station by C-130 aircraft from the US McMurdo Station, and a large amount of densifier was added to hole No. 5G-1 to raise the fluid density. Drilling was continued, and reached 3350m by January 1996 using the KEMS-132 drill with a cutter diameter of 135 mm. The hole was enlarged to 137 mm every 25–30 m. Increasing difficulties with chip collection in the warmer ice after 3000 m resulted in shorter cores and the eventual stoppage of drilling (Kudryashov and others, 1998a, b, 2000, 2002). A traverse consisting of 16 vehicles started from Mirny to Vostok on 12 November 1995, but mechanical problems with the vehicles forced a decision to cancel the traverse at the 645 km mark. For the first time in Soviet and Russian Antarctic expeditions, a traverse failed to reach Vostok station. On 24 January 1996 all the people were evacuated by C-130 aircraft and Vostok station was closed down again. Future drilling operations were to be reduced to short Antarctic summer seasons.
42nd RAE (summer season 1996/97)
Vostok station was reopened and the drilling of hole No. 5G-1 was resumed with the KEMS-132 electromechanical drill. The drill head was equipped with special shoes to limit the pitch of the cutters, which allowed drilling operations to resume. However, at the end of this season the decrease in the length of the drilling runs (up to a complete stoppage of coring) reoccurred. It is worth noting that in the two latter cases the stoppage was not associated with jamming of the drill head. Drilling efficiency was reduced dramatically, and sticking of the drill head due to the presence of ice chips at the hole bottom was occurring immediately after the beginning of a drilling run. Nevertheless, hole No. 5G-1 reached 3523m by the end of the season at the end of January 1997 (Kudryashov and others, 2002).
43rd RAE (summer season 1997/98)
Despite the improvements that have been brought into the design of some units of the drill, at the beginning of the 43rd RAE season the drilling was unstable again. Only after certain changes in the geometry of the cutter, aimed at decreasing sticking of the ice chips to the drill head, could the drilling be continued. To prevent icing on drill-head cutters, the clearance angle was increased to 15˚; in addition, the cutters and the body of the drill head were covered with a thin Teflon layer. These measures significantly increased the efficiency of ice destruction and chip removal from the hole bottom. As a result, ice coring during the 43rd RAE season was performed in the routine mode of operations. Drilling was stopped at 3623m in January 1998, about 130m above Vostok Subglacial Lake (Kudryashov and others, 2002).
During this drilling season, at 3538m depth the drill passed from meteoric ice into accretion ice which formed by freezing of the subglacial lake. There was no visible change in drilling mode except the appearance of oversize ice pieces at the bottom of the hole (see next subsection).
Between 1998 and 2005, borehole geophysical measurements were performed.
51st RAE (summer season 2005/06)
After 8 years, hole No. 5G-1 was reopened for drilling. At the beginning of the summer season, the drilling equipment and the hole itself were carefully inspected. On 31 December 2005, the first productive run was made by the electromechanical drill KEMS-135, and 0.5 m of new core was recovered. The new geometry of cutters for drilling of ‘warm ice’ was tested: the bottom-side form of the cutters had a dihedral shape, which allowed the clearance angle to be increased up to 30˚. This gave stabilization to the drilling process. As a result, hole No. 5G-1 was deepened to 3650.2 m, with an average core length of 0.7–0.8m per run (Fig. 16). On 25 January 2006, the seasonal operations at Vostok ceased.
The hole diameter was measured by a special borehole logger of lever type with a precision of 0.2 mm. The diameter change over time was insignificant and lay in the range of measurement accuracy (Fig. 17). The drilling-fluid pressure in the hole was measured, and the pressure difference on the hole walls was estimated (Fig. 18). The pressure difference at depths close to the hole bottom is near zero, which indicates satisfactory compensation of the ice overburden pressure. The liquid level is at 95 m depth; the average fluid density is 928 kgm–3.
Drilling performance in ‘warm ice’
Electromechanical drilling of ‘warm ice’ is characterized by sudden losses of drilling progress, which are caused by the rapid gluing together of ice cuttings forming ice spots and rings on the surface of the drill equipment (especially near the drill head). This blocks the fluid circulation, and the normal drilling process is stopped. If the drilling is continued, there is a high risk of getting the drill stuck. This effect was noticed in all recent drilling projects in Greenland (NorthGRIP) and Antarctica (Dome C, Dronning Maud Land and Dome F).
The first problems that could be connected with the peculiar properties of ‘warm ice’ appeared in hole No. 5G-1 at depths near 3000 m. The instability of drilling progressively increased with depth. In particular, unexpected jamming of the drilling head often occurred even at low drilling pressures, that is, at penetration speeds of about 1 mh–1 or less. This was accompanied by significantly shorter drilling runs. At depths below 3480 m, the efficiency of drilling was reduced dramatically, and sticking of the drill head due to the presence of ice chips at the bottom of the hole occurred immediately after beginning a drilling run.
We explain our problems in terms of the changing ice properties, in particular by changes of ice crystal size and ice surface structure. In Figure 19, two plots – run length and crystal size vs depth – are combined (data on ice crystal size are from Reference Lipenkov and BarkovLipenkov and Barkov (1998) and Reference Lipenkov, Barkov and SalamatinLipenkov and others (2000)). The correspondence between these plots is clearly visible: increasing ice crystal size leads to decreasing run length. Certain improvements were brought into the design of the drill head and chips chamber that allowed the drilling operations to proceed, but the tendency toward decreasing run length continued.
The ice cuttings of fine-grained ice with crystal sizes less than 5 mm consist of chips with dimensions of 1–2mm and more. The cutting process of the coarse-grained ice is different: the dimensions of the ice cuttings are much less, not exceeding 0.5 mm. At the same time, many very small chips like ice fines were formed. The fine chips easily plugged the filter in the chips chamber, sharply increasing the hydraulic resistance in the drill circulation system and decreasing the fluid flow rate. The drop in the flow rate caused ice plugs to form in the most critical places of the drill, i.e. near the cutters and the drill head.
This situation is exacerbated by water appearance on the ice surface. According to the theory of Reference FletcherFletcher (1970), on the surface of ice with a temperature of –6˚C the quasiwatery layer with a thickness of near 10Å(10–9 m) appears instantaneously, and at temperatures near 0˚C the thickness of the layer increases to several hundred ångstroms. Fletcher’s conclusions were made for ice under atmospheric pressure. Taking into account the depression of the ice melting point under pressure, we can estimate the change in adhesion properties of the ice starting from depths near 3000 m.
Another problem with coarse-grained-ice drilling was the formation of oversize pieces of ice that were split off the core while the core was broken from the bottom by core catchers. Higher in the hole, such ice pieces were fine-grained and easily broken by drill-head cutters. Breaking the coarse-grained ice pieces required a considerably higher force impact. Ice pieces with dimensions larger than clear openings cannot be destroyed by the cutters, and so initiate ice-plug formation in the space between two cutters (Fig. 20). Even though the two other openings of the drill head were still unblocked, eventually the penetration stopped (our experience showed that it was possible to drill no more than 50–100mm having such an ice plug in the opening between cutters).
We can imagine the following interaction modes between cutters and oversize pieces of ice. If the oversize ice pieces enter the opening of the drill head, it is impossible to penetrate at all, even at a cutter load equal to the drill weight (Fig. 21a). To avoid such a mode it is necessary to limit the space between cutters with the help of a fixed stop installed between cutters. The size A (Fig. 21 b) should be less than the clearance between the core and the inner surface of the core barrel. In this case, the destruction of oversize pieces of ice should proceed as shown in Figure 21b–e. The oversize pieces of ice cannot enter the opening of the drill head and so begin to be cut by the cutters. The ice cuttings produced look like thin plates with a width equal to cutter width and a thickness of a few millimeters. During experimental drilling with a modified drill head, we have repeatedly found such ice plates in the chips chamber.
The width of these plates is not small enough for them to pass through the clearances of the drill circulation system. To decrease the width of such ice plates, special grooves were made in the bottom side of the cutters, dividing the edge of the cutters into two working areas (Fig. 22).
Planning Penetration and Sampling of Vostok Subglacial Lake
Since 1998, a technique for the continued penetration of hole No. 5G-1 to Vostok Subglacial Lake has been studied (Reference VerkulichVerkulich and others, 2002). We propose to access the lake and sample the water in three stages, as follows (Fig. 23).
The first stage includes an additional deepening of hole No. 5G-1 to a depth near 3720 m, leaving about a 30m thick ice layer to prevent contamination of the lake by the drilling fluid. This can be accomplished with electromechanical drill KEMS-135, which has been successfully employed here. Then a new, ecologically friendly liquid (silicone oil) is delivered to the hole bottom by a special tanker. It is anticipated that this hydrophobic liquid, being heavier than the drilling fluid and lighter than water, will create a 100 m thick ‘buffer layer’ in the bottom part of the hole. The hydrostatic pressure at the bottom of hole No. 5G-1 should be slightly lower than the overburden ice pressure.
The second stage is drilling up to the ice–water interface. This will be carried out by thermal drill TBPO-132 in one operation. Two versions of thermal drill TBPO-132 (without container for subglacial water and with it) are shown schematically in Figure 24. At the instant the tip of the thermal head touches the ice–water interface, a special penetration gauge gives a signal to the surface and the packer of the thermal drill is automatically turned on. The packer is needed for separation of the hole and lake at the instant of penetration.
If the special sterilized container is used, the valve is opened and the container is filled by subglacial water. When the container is full, the valve is closed. After estimating the actual difference between the pressures in the hole and in the lake and maintaining that pressure difference in the range 3–4 bar, the packer is turned off and the water from the lake is allowed to enter the hole (this moment is shown in Fig. 23, stage II). The thermal drill TBPO-132 will be pulled up. It should be possible to allow lake water to enter into the hole to a height of 30 or 40 m and to freeze.
The third and last stage will be conducted after confirming that the freezing in the hole is finished. Coring of the frozen lake ice can then be done with the electromechanical drill KEMS-135 down to 10–15m above the ice– water interface.
The project ‘Basis and Design of an Environmentally Clean Penetration to Lake Vostok, Antarctica’, prepared by SPSMI and AARI, was approved by the Ministry of Nature Resources of the Russian Federation (Order No. 257, 26 March 2001). The Russian project for the penetration to Vostok Subglacial Lake was presented to the 26th Antarctic Treaty Consultative Meeting in Madrid, Spain, in June 2003. The project for the penetration to Vostok Subglacial Lake has started. The distance between the hole bottom and the ice– lake interface is near 100m now. In the 2006/07 summer season and the winter of 2007, additional drilling of the hole to a depth of near 3720m is planned.
Acknowledgements
The report is dedicated to all ‘miners’ who tirelessly spent so many years and expended so much effort to further the cause of glaciology. From the very beginning, Vostok drilling was led by B.B. Kudryashov, who passed away on 12 April 2002. Since 1999, deep drilling at Vostok station has been carried out within the framework of the Federal Targeted Program (FTP) ‘World Ocean’, subprogram ‘Antarctica’, project 4 ‘Deep ice coring, paleoclimate research and Subglacial Lake Vostok exploration’. The authors thank H. Ueda for help in organizing and correcting material regarding the Vostok drilling. We also thank C.R. Bentley for very constructive and pertinent remarks and for editing this paper.